Milford Haven Bridge Collapse.ppt
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Transcript Milford Haven Bridge Collapse.ppt
Milford Haven Bridge
Collapse
Cathal Kennedy
Terence Meade
Sara Farivarz
Padraig O’Rourke
Contents
Introduction
Milford Haven
Bridge
The Collapse
Results
Conclusion
Introduction
Box Girders:
used for large 2nd
moment of area &
torsional resistance
Hard to analyse,
however
One of 4 similar
bridges that failed
from 1969 - 1971
Milford Haven Bridge
Box
Girder design
Consisted of 7 separate spans from
77m to 312m in length
Built by being cantilevered out from
piers
Sections then welded or bolted to
end
The Collapse
Occurred when
launching deck
section across
Stresses during
construction are
very different and
often larger than
when the bridge is
completed
Continued
occurred during
launching a preassembled deck
section towards the
second pier.
subjected to bending
moments and vertical
shear forces.
buckling of diaphragm
lead to buckling of
lower flange.
Load before failure
9700kN
Results
Committee
of Inquiry concluded that
BS153 was inadequate
Merrison committee sets rules which
become the basis for BS5400
West Gate Bridge strengthened but
collapsed 2 months after killing 32.
Conclusion
Ultimately caused
by human error –
failure to anticipate
effects during
construction
Highlights need for
engineers to fully
understand
principles behind
construction