Automated Recovery Boiler Sootblowing Control System Barbara G. Haley; B.A., Accounting; C.P.A. University of South Alabama; Mobile, AL Floyd I.
Download ReportTranscript Automated Recovery Boiler Sootblowing Control System Barbara G. Haley; B.A., Accounting; C.P.A. University of South Alabama; Mobile, AL Floyd I.
Automated Recovery Boiler Sootblowing Control System Barbara G. Haley; B.A., Accounting; C.P.A. University of South Alabama; Mobile, AL Floyd I. Lawrence; B.S., Electrical Engineering University of Iowa; Iowa City, IA Brad S. Carlberg, P.E.; B.S., Mechanical Engineering Washington State University; Pullman, WA Ford, Bacon & Davis, LLC Mobile, AL James A. Johnson; B.S. Electrical Engineering Louisiana Tech; Ruston, LA Ford, Bacon & Davis, LLC Monroe, LA 2001 TAPPI PCE&I / ISA PUPID Joint Conference March 27, 2001 Page 1 Automated Recovery Boiler Sootblowing Control System The mill’s OTHER Recovery Boiler sootblowers were already controlled by a pair of redundant PLC’s The existing sootblower panel was beginning to take more maintenance time - “it was wearing out” Operators wanted “better” control: sootblower sequences, etc. E&I technicians wanted “better” diagnostics to help find failed field devices Superintendent wanted better tracking of failed field devices to determine cause of shutdowns 2001 TAPPI PCE&I / ISA PUPID Joint Conference March 27, 2001 Page 2 Automated Recovery Boiler Sootblowing Control System Team Effort Assured Smooth Start-Up PLC Code Programming Backup HMI Programming DCS Programming Installing New I/O Cables Dynamic Simulation in PLC tested PLC code Prior to Start-up / Commissioning Cutover Completed in Two-Week Yearly Shutdown Recovery Boiler & Sootblowers Started Up On Time 50% of team on-site at startup 2001 TAPPI PCE&I / ISA PUPID Joint Conference March 27, 2001 Page 3 Automated Recovery Boiler Sootblowing Control System UNEFFECTED Field Device’s NEW REDUNDANT PLC’s UNEFFECTED UNEFFECTED Intermediate Junction Box in MCC New I/O Cables from MCC Existing I/O Cables from MCC “Blue Hose” REMOVED Sootblower Control Panel 2001 TAPPI PCE&I / ISA PUPID Joint Conference Back-Up HMI NEW Existing DCS Added NEW Screens March 27, 2001 Page 4 Automated Recovery Boiler Sootblowing Control System The Automated Recovery Boiler Sootblower System Operates basically the same as the original panel-mounted controller; EXCEPT for greater visibility The Automated Recovery Boiler Sootblower System Operates the Same on Both the DCS Operator Interface and the Redundant, Backup, Plasma Screen Operator Interface The Operator Interface and the DCS Are Talking to the Same PLC and Reading the Same Points The PLC Does Not Care Which System Sends It Information, It Will Simply Process the Information As It Is Received 2001 TAPPI PCE&I / ISA PUPID Joint Conference March 27, 2001 Page 5 Automated Recovery Boiler Sootblowing Control System Six (6) Display Screens: Sootblowing Control Manual Mode Blower Select Automatic Sequence Blower Out of Service Limit Switch Monitoring Help Screens Alarm screens 2001 TAPPI PCE&I / ISA PUPID Joint Conference March 27, 2001 Page 6 Automated Recovery Boiler Sootblowing Control System Main Display Screen 2001 TAPPI PCE&I / ISA PUPID Joint Conference March 27, 2001 Page 7 Automated Recovery Boiler Sootblowing Control System 3 PRE-DETERMINED SOOTBLOWING SEQUENCES ALL Sootblowers in ASCENDING Order Economizer Sequence (1-32, then 1-52) Generator Plugging Sequence (5-8,15-18,25-28,1-52) FOUR (4) OPERATING MODES Steam Mode Automatic Control Mode Steam Mode Continuous Control Mode Sequence Continuous Cycle Mode Sequence Single Cycle Mode 2001 TAPPI PCE&I / ISA PUPID Joint Conference March 27, 2001 Page 8 Automated Recovery Boiler Sootblowing Control System Manual Mode Blower Select 2001 TAPPI PCE&I / ISA PUPID Joint Conference March 27, 2001 Page 9 Automated Recovery Boiler Sootblowing Control System Automatic Sequence Sootblower Out of Service 2001 TAPPI PCE&I / ISA PUPID Joint Conference March 27, 2001 Page 10 Automated Recovery Boiler Sootblowing Control System Limit Switch Monitoring 2001 TAPPI PCE&I / ISA PUPID Joint Conference March 27, 2001 Page 11 Automated Recovery Boiler Sootblowing Control System Alarm Notification Screen 2001 TAPPI PCE&I / ISA PUPID Joint Conference March 27, 2001 Page 12 Automated Recovery Boiler Sootblowing Control System Help Screens 2001 TAPPI PCE&I / ISA PUPID Joint Conference March 27, 2001 Page 13 Automated Recovery Boiler Sootblowing Control System I/O Count 56 Digital Input - 4 ea 16 point cards (4 for Even/Odd Fwd/Rev & 52 for each Soot Blower) 156 Digital Output - 11 ea 16 point cards (3 limit switches for each of 52 Soot Blowers) I/O Racks 2 16-slot racks - with single slot addressing with scanner cards in each rack Communication Only 2 channels used (1A-DH+ & 1B-RIO) Communicates to DCS via Extended PLC Gateway 2001 TAPPI PCE&I / ISA PUPID Joint Conference March 27, 2001 Page 14 Automated Recovery Boiler Sootblowing Control System CONCLUSIONS Pre-Existing, Hard-Wired Field Devices UNAFFECTED Pre-Existing, Stand-Alone Sootblower Panel REMOVED Redundant PLC’s Assure Constant Control DCS and Backup HMI Assure Constant Visibility DCS Continuously Collects the Plant’s Real-time Process Data Operators Have Greater Access to That Real-time Process Data 3 Strategic, Pre-Determined Sootblowing Sequences ALL Sootblowers in ASCENDING Order Economizer Sequence (1-32, then 1-52) Generator Plugging Sequence (5-8,15-18,25-28,1-52) Easy to implement 15 more sequences by “fill-in-the-blanks” E&I Technicians Can Quickly Find and Troubleshoot Failed Field Devices From the Alarm Display Better Control of Sootblowers Optimally Operate the Recovery Boiler. 2001 TAPPI PCE&I / ISA PUPID Joint Conference March 27, 2001 Page 20 Automated Recovery Boiler Sootblowing Control System MORE CONCLUSIONS The Plant Saved Resources (i.e.; Steam) and Reduced Plant Operating Costs Significantly by “Smoothing” Steam Demand The Plant Only Blows Soot When It Is Needed, and Only in the Necessary Locations (i.e.: Economizer or Generator Tube Banks) Automated Sootblowing Improves Boiler Heat Rate, Minimizes Soot Accumulation, Improves Overall Boiler Efficiency, and Balances Blowing Sequences The Plant Is Able to Avoid Unnecessary Steam Usage and Opacity Spikes Plant Equipment Life Was Extended and the Plant Now Avoids Forced Outages Due to Soot Accumulation The Operators Can Use the Additional Real-time Process Data and Alarm Management Display to Schedule Sootblowing Sequences and Optimally Operate the Recovery Boiler 2001 TAPPI PCE&I / ISA PUPID Joint Conference March 27, 2001 Page 21 Automated Recovery Boiler Sootblowing Control System FUTURE RECOMMENDATIONS Add Additional Sootblowing Sequences By Modifying The PLC Code Implement Smart Sootblowing By Implementing Advanced Control Software in DCS Utilizing Instrumentation in DCS 2001 TAPPI PCE&I / ISA PUPID Joint Conference March 27, 2001 Page 22